Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
A/F mixture
by: twodogsnme - Jun 2, 2015 22:30:01 GMT -6
via mobile
Post by twodogsnme on Jun 2, 2015 22:30:01 GMT -6
Hey katastruff..where can I get a manual enrichner like in the pic? Could u post a Link? Thanx
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
A/F mixture
by: twodogsnme - Jun 2, 2015 19:30:23 GMT -6
via mobile
Post by twodogsnme on Jun 2, 2015 19:30:23 GMT -6
Thanx Cyborg n Diver..checked enrichner..no fuel coming from there..gonna check/change pilot jet tm..hopun this will take hesitation out of start..got great acceleration all the way thru throttle now..wwhhooppee!!..if I can get bottom end responce fixed I'm done messin w/it..lol..keep the rubber down
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
A/F mixture
by: twodogsnme - Jun 2, 2015 8:47:23 GMT -6
via mobile
Post by twodogsnme on Jun 2, 2015 8:47:23 GMT -6
I removed enrichner per post here..used gasket material to block holes..even blocked large opening where enrichner needle went..may have found problem.. Lot of slack at throttle to carb cable..tightened it up seems to make diff..still got A/F screw at 1/4 turn from closed..runnin fine performance wise.. Just concerned that its too lean n I'm gonna burn engine up..how bout a recommendation fer a good cdi/ coil? Or are they basically all the same? Thanx n keep the rubber down
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
A/F mixture
by: twodogsnme - Jun 1, 2015 12:46:33 GMT -6
via mobile
Post by twodogsnme on Jun 1, 2015 12:46:33 GMT -6
Hey scooter ppl..Alley,Bashan,etc..I have a Tao Tao 150,I have installed a 26mm carb(rejetted w/110 main),added cold air intake(took stock airbox off),removed enrichener,n have a heck of a time tryin to find right A/F mixture. I have started 2 1/2 out n adjusted per 4t carb tuning posted here. It only runs great when A/F screw is bout 3/4 turn ccw from closed. I understand that these need to run a lil rich but when I try this it runs crappy..my question is since I have increased air inflow, would I still need to adjust A/F screw as directed?.. I should add that I have a "unrestricted" cdi n coil installed too.my top end is great(50+)..n she accelerates well..except from stop..lil hesitation then she runs right out. Any suggestions? All replays will b appreciated.. Also can y'all reccommend a good quality cdi/coil setup? Provide link if possible...I got mine off interweb from scorpion products.thanx n keep the rubber down
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 28, 2015 1:34:41 GMT -6
Please c my new post concerning new carb n performance at 50-200cc forum..need alleyz cyborgz n anyonez help w/this..thanx n keep the rubber down
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 28, 2015 1:29:32 GMT -6
Ok scooterppl..I just put in a 26mm carb n a stainless cold air intake/air filter..turned air fuel screw 2 1/2 turns..adjusted to set idle..now I have good mid n high acceleration.. But it bogs n recovers after its warmed up..only happens from slow down/stop..when I give it a lil throttle it bogs fer a sec or two then picks up..more throttle better performance.. Any thoughts on this? PS installed new plug n ran fer a few (20 mins)..pulled plug..some soot..suspect a lil rich but understand this is better than lean..mayb adjust carb needle? All replys will b appreciated.. Keep the rubber down
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 22, 2015 23:12:49 GMT -6
Did ya c the lil sign that said "wholesale - dealer only"? Mayb the prob...
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 22, 2015 23:00:34 GMT -6
Ok folks changed oil..no motor honey this time..no smoke or noticeable decrease in compression or power..think the scooter gods have blessed me..ordered new 26 mm carb n intake manifold..figger this one comes w/correct size main jet..lol..also took breather box out/off n installed stainless air intake tube w/generic air filter..runnin ok but bogs down at lil past half throttle.. Hoping new carb will rectify..it still will do 50 very comfortably.. Very pleased w/Tao Tao brand so far..now to the headlights..will keep posting progress..keep the wind in yer face n the rubber down
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 21, 2015 11:49:19 GMT -6
U too Clonedrone! Oil change in 100 mi..no motor honey this time..fingers crossed that all is well..will post ltr
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 21, 2015 11:47:37 GMT -6
Thanx fer the feedback(sarcastic as it was) on the carb screws..gonna order 26mm carb n intake manifold n b done w/it..Thanx Cyborg..I value yer opinion on these matters..keep the rubber down y'all
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 18, 2015 21:57:09 GMT -6
Well tried the reject( got airbox out n radiator hose/filter in)but the silly Chinese cut the heads off the carb bowl bolts!!only way I can figger to fix is drill em out?!!..any suggestions? Thought bout just orderin a new carb..mayb 28mm..any thoughts on that idea? All replays will b appreciated
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 18, 2015 21:52:22 GMT -6
Got 1300+ on it now..oil change due at 1600..will not use motor honey this time..fingers crossed..will update in a couple daze..keep the rubber down y'all
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 15, 2015 23:56:47 GMT -6
No broken rings..seems to b runnin fine now.. Got giddy up n go n same idle I had b4...no oil in breather box..not loosin any either..bn bout 89 mi n still register same on dipstick..gonna re jet n take stock airbox out tm..gonna use a radiator hose n PVC n a generic air filter..hoping to let her breath better.. Will post later..thanx fer the feedback n opinions..keep the rubber down
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
Post by twodogsnme on May 12, 2015 0:01:50 GMT -6
Well folks thanx fer the feedback..I put ring sealer in with the new oil(by the way this is third oil change..first was b4 I even rode it..second at 500 mi n this one at 1100)..so far no more smoke...it also runs just like it did..same rpm level..same giddy up..I really can't tell a difference..will look fer oil in breather tube tho! Will check oil level too. Also a lil more info..I had to come to an abrupt stop from bout 40 mph right b4 I noticed smoke from tail pipe..think mayb the sudden stop forced oil up into manifold n out pipe? ( just hoping/guessin)...will keep postin progress..gonna order new head kit anyway..its under warranty so won't cost much..just some elbow grease n a few scrapes..keep the rubber down n the wind in yer face
|
|
Doc's Anything Goes
Currently Offline
Posts: 58
Likes: 0
Joined: Apr 7, 2015 0:08:58 GMT -6
|
auto choke?
by: twodogsnme - May 10, 2015 8:30:01 GMT -6
via mobile
Post by twodogsnme on May 10, 2015 8:30:01 GMT -6
Hey Alleyoop..can you post some pics of yer setup?..thanx n keep the rubber down
|
|